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One other person told me to check my freq in the firmware and sure enough I had missed changing the default of 8 Mhz to the correct 12. Everything works great now.
Thanks for the help.
I'm doing the initial steps to start up my new Voron 2.4 build. The steeper buzz test go great but as soon as I try and home either x or y the system shuts down with an mcu shutdown error.
This is my first build and I'm sure I do not have the printer.cfg file correct.
Any suggestions?
New build, I get past the "stepper buzz" with no problems but when I do the XY Homing check, on either motor, the gantry moves up (no X or Y movement) stops and shuts down Klipper with the "MCU 'mcu' shutdown: Timer too close" message.
What am I doing wrong?
Another newbie question. This is my first jump into Linux so I'm unfamiliar with editing the printer.config file. Voron says :
Additional Changes: MainsailOS only
1. Add the following entry to your printer.cfg: [include mainsail.cfg]
Does it matter WHERE I add it? In the beginning, end, ???
I pretty much figured as much, especially since I didn't find that small piece of 4x2 until AFTER I assembled the head! ;) And I thought I had gone through everything before I started....
Thank you for the help!
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